Dune Bug-E 

Controller/Wiring/Road Test - Part 5 ...

May 2010

 


Part 4 was focused on the drive train and the rear swing-arm assembly, and a lot of misc detail work on the front ie; brakes, steering, seats and wheels...

 

With the motor & wheels removed, the rear-end was blasted with a coat of primer and painted the standard camo colours...

This base coat will be re-painted yet again with grasses and local foilage as spring progresses and they become available.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The cross-bar that the shock mounts are welded to had a second bar with braces welded into place (not clear in this image)...

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Both Battery Banks were installed, and a pair of tie-down straps cut, bent and drilled to fasten them into place.

 

 

 

 

 

 

 

 

 

 

 

 

 

The 3KVA UPS/Charger is installed into it's racking and bolted into place.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The image to the right are the "Electronics" that will control the motor...

After surveying the market and numerous Emails, I ultimately ordered a Kelly Controller's KD48500 Controller w/Main Contactor, F/R Contactor and foot throttle assembly.

Although I'd implied earlier on this page (or perhaps the Endless Sphere Forum's) that I'd be revisiting & upgrading and PicOx Open Source controller for the Dune Bug-E, the reality is that I'm running out of time if I want to make use of this unit before the snow flies again.

 

 

 

 

 

 

 

 

 

 

The foot throttle assembly as bolted down, is reasonably comfortable (considering how cramped the quarters are within the cabin).

If I could find fault with this unit it would only be the poor fit between the pedal assembly and the Pot-Box itself.

To make a secure mount I had to wrap the shaft with some electrical tape and cut open the "C" in the pedal casting so that it could be tightened down and remain secure.

 

 

 

 

 

 

 

 

 

The shop was cleared, swept, and wiped down to clean-up the layer of metallic dust that has accumulated over the last few months.

The welder, clamps, and misc materials are stored away, and the bench re-configured for the wiring of the controller...

 

 

 

 

 

 

 

 

 

 

 

 

 

The documentation that came from Kelly was clear and easy to follow.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

One feature I wanted to incorporate from the beginning of this project was the ability to run the motor controller and/or the 3KVA Inverter independently, as well as charging the banks individually as required.

The image to the right is of the "Toolpath" used to cut out a series of 1/4" Nylon pieces that would be laminated together with 4 heavy copper buss-bars to form a switch assembly.

The Nylon was cut at a 45 inch per minute feed rate using a 0.062" end-mill bit. By cutting at 0.020" per pass the cutter never clogged or missed a step.

 

 

 

 

 

 

 

 

 

 

 

Cutting the pieces out on the CNC Mill.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The cuts were made to a depth of 0.220" leaving 0.030" to be trimmed out with the band-saw and a sharp exacto-knife.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

This shot is of the switch partially assembled.

The 3/4" by 3/8th" buss-bars are notched such that the small nylon spacers that allow a gap for the Knife to swivel in are securing the buss-bars from moving once the switch is completely assembled.

 

 

 

 

 

 

 

 

 

 

 

 

 

The "Hot or B+" lines from the Battery banks are bolted to the Knife-Bars.

The Buss-bars had "V-Cuts" machined to mate to "Wedges" that were machined in to the Knife-Bar edges, to maximize the contact area when engaged.

For now the knife switches are secured in position by simple rubber bands.

This has been working very well, and most likely will remain.

 

 

 

 

 

 

 

 

 

This is a view from the back of the controller with the cable harness that ties the keyed ignition, throttle, brake sensor and Fwd/Rev switch.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

All Load carrying cables (from Battery banks thru the controller onto the motor) are AWG #4 welding wire.

Each cable end is crimped and soldered to a homemade brass end lug, taped and labeled as assembled.

 

 

 

 

 

 

 

 

 

 

 

The charging circuit to the battery banks is AWG #8 with an Anderson connector that can be pulled either for servicing or if things go wrong.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

For now I've just mounted the Fwd/Rev Switch and Keyed Ignition on the original dash-brd. 

This will eventually be replaced with a wood console and a pair of analog meters to display the Voltage (State of Charge) on the Battery Banks and a Current meter, as well as a Temp sensor that will be mounted on the motor.

 

 

 

 

 

 

 

 

 

 

 

At this point the Dune Bug-E is up & running, and has had 8 or 9 test drivers without any issues ie; intermittent power of general failure while driving.

The Home Brew High Current switch was one area that I'd had concerns about but they proved needless.

The slip differential in the rear-end will be welded or fixed to approximate a Posi-track or solid rear drive, as there is no flex in the frame or swing-arm, so one of the rear wheels is prone to getting hung-up spinning in the air...

 

 

 

 

The Kelly Controller is still set at it's factory defaults, as there was a gap in communications between me and the Kelly Sales Staff regarding an SCI to RS-232 adapter that allows the PC to talk to the controller.

Given that the controller is rated at 48V 500Amps the usage has been on the "Light Side" for fear that I damage the motor. Ideally I'd like to dial-in a bit more responsive throttle over the full arc of it's movement (the first 1/4 of it's travel is dead), and set an upper limit of 200Amps initially on the controller, until I add a temperature monitor to the motor to ensure it doesn't over heat.

While I have the gear-box dis-assembled, there is a slim possibility of re-gearing it internally for a much higher top-end. Presently it has tremendous torque in all three forward gears, but is far slower than I'd calculated. After reviewing the spreadsheet I found that I'd made an error in one equation that grossly over estimated the top speed of the buggy. If re-gearing internally is not an option, I'll add a jack-shaft and sprockets to bump-up the speed with an aim towards a 35 to 40Km/hr top speed in 3rd.

(Video to be posted by May 10th 2010)

 


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